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  1. #1
    Join Date
    Feb 2005
    Location
    Northern CA
    Posts
    139

    Dead coolant pump on Turnpro - help!

    Sort of continuing this thread.
    http://www.hobartwelders.com/mboard/...ad.php?t=12395

    Everything on my saw worked great... until I turned it on this morning and the pump wouldn't pump. The pump has 120V going to it, but no love. After kicking and screaming at it, and trying like heck to break free the screws that hold it together - I gave up and called Enco. In about five minutes, they have a new pump on their way to me under warranty. Nice!

    But... what the heck happened here? I just can't imagine what would make the thing up and die so fast. Now that I know a new one is on the way, I think I'll give it an even harder try (maybe with some real heat this time??) to get this old one apart to see what the heck is going on. Any guesses? Any tips on getting it apart?
    - Darell
    HH180, Cutmaster 38, Miller Xlix Elite, TurnPro 7x12 Horiz bandsaw.

  2. #2
    Join Date
    Jan 2004
    Location
    Browns Valley, CA
    Posts
    8,518
    Does the motor turn? Is it warm? If it's not turning, and it's warm, the pump is siezed. If it's not turning and it'sNOT warm, the motor is kaput!

    Hank
    ...from the Gadget Garage
    MM 210 w/3035, BWE
    HH 210 w/DP 3035
    TA185TSW
    Victor O/A "J" series, SuperRange
    Avatar courtesy of Bob Sigmon...

  3. #3
    Join Date
    Feb 2005
    Location
    Northern CA
    Posts
    139
    Hi Hank. Fortunately, I can answer everything now.

    I decided to take no prisoners, since my new one is on the way, and I have nothing to lose. First off, no - nothing was turning, nothing was warm, nothing was making any noise. 120V was getting the the wires that enter the motor housing. The shaft spins easily by hand. That's all I knew before I started. So with a big enough hammer and some heat, I was able to pull the motor apart and and carefully dissect it. The thing looked perfect inside and out. Everything was snug and moved freely. All electrical connections seemed sound. Frustrated in not finding anything obviously amiss, I put it all back together, and hooked it up directly to 120V - worked! Put it back in the saw, and turned it on. Presto - coolant all over the freaking shop (since I had the arm vertical and the ball**** all the way open)! But I was happy anyway.

    I have NO idea what was going on, but something in the reassembly has fixed the darn thing. Too late to stop the new one coming, but I don't feel too bad. Who knows how long this one will keep spinning? For now though, it seems that I'm good to go.

    Thanks for the response.
    Last edited by darelldd; 06-13-2005 at 11:00 PM.
    - Darell
    HH180, Cutmaster 38, Miller Xlix Elite, TurnPro 7x12 Horiz bandsaw.

  4. #4
    Join Date
    Mar 2005
    Posts
    90
    Shortly after getting my Turnpro, the coolant stopped pumping. The motor would turn but no pumping. I took everything apart and all looked good. Put it all back together and still no coolant. After "sleeping on it" it occurred to me that maybe, just mayber the water level was too low. It looked like there was enough water but I filled it all the way up anyway and "presto" coolant flowed all over the place. Doesn't sound like that was your problem. I most often overlook the obvious and tear it all down first. Wasted four hours trying to fix it.
    Millermatic 210 w/Spoolgun
    Smith "Airline" O/A
    Hornell Speedgall 9002v Helmet
    Turn Pro 7 x 12 Band Saw
    Cummins Mini Lathe
    Cummins Mini Mill
    Hon Leather Office Chair...where I do most of my work.

  5. #5
    Join Date
    Sep 2002
    Location
    Central Kali
    Posts
    5,292
    A good pump is The Little Giant submersible. They come in different sizes. I have used them on swamp coolers instead of the stock cheapies that come with them. I like being able to stick the whole pump under water, including the cord.

  6. #6
    Join Date
    Feb 2005
    Location
    Northern CA
    Posts
    139
    I'll keep that pump idea in mind for if these thing goes South two more times.

    As for coolant level, that was the first thing I checked actually. I figured I'd have lost quite a bit in evaporation since it has been HOT in the shop lately. But no - plenty of coolant. The second thing - which should have been the first - was to see if the pump was spinning. Easy to tell since there is a window in the top with a red dot that spins - and the shaft is exposed. When I realized that wasn't moving at all, I knew something was bad.
    - Darell
    HH180, Cutmaster 38, Miller Xlix Elite, TurnPro 7x12 Horiz bandsaw.

  7. #7
    Join Date
    Feb 2005
    Location
    Northern CA
    Posts
    139
    Hey guys. Remember this problem? Well, it is back.

    Here's what I've learned: If I use the pump every day, all is good. If I let it sit for a few days or a week, the pump is siezed on the impeller end. I can break it free by twisting the shaft manually a few times, then it is good to go again. I have my replacement pump that was sent to me, but I don't want to put it in until I figure out what the heck is going on.

    It would seem that the pump is picking up cud from the coolant? Of course there are plenty of shavings in the tank. But it isn't THAT bad! How often do you guys change the coolant?
    - Darell
    HH180, Cutmaster 38, Miller Xlix Elite, TurnPro 7x12 Horiz bandsaw.

  8. #8
    Join Date
    Sep 2002
    Location
    Central Kali
    Posts
    5,292
    When I last used a pump on the bandsaw, I made a filter out of a couple of layers of window screen over the drain hole to the tank. I used magnets to hold the screen which also picked up a lot of the metal.

  9. #9
    Join Date
    Jul 2005
    Posts
    3

    coolant pump

    Hi there;
    I've killed a couple pumps. Usually a chip gets caught in the impeller, I now use a screen and a magnet to keep the chips from getting in. I replaced mine with a nice little fully submersible, bought through Grainger. Anything will work so long as you look at the gpm and head.

  10. #10
    Join Date
    May 2005
    Location
    Richmond, Virginia
    Posts
    5,316
    He, he, he. Reminds me of the time I changed the youngun's diaper, and took my time doing it. "Coolant all over the freaking" bedroom was more like it.
    --- RJL ----------------------------------------------

    Ordinarily I'm insane, but I have lucid moments when I'm merely stupid.
    -------------------------
    DialArc 250
    SyncroWave 250 w/Coolmate 3
    SP-175+
    TA 161STL
    Lincwelder AC180C circa 1950
    Victor & Smith's O/A
    Dayton (Miller) spot welder
    1200 sq.ft. of garage filled with crap
    A kid that can actually run the stuff +++

  11. #11
    Join Date
    Feb 2005
    Location
    Northern CA
    Posts
    139
    Thanks guys.

    Well, I swapped in the new pump (I mean what the ****, I have it!) and I had the magnet idea all by myself. I tossed on in the well. But I like the idea of putting it up in the catch screen (entry to the well) even better. I'll even go so far as to put it in a little zip-lock first so it is easy to get the metal off of it.

    Another god thing that came out of this is that I lengthened the power cord and even put a quick disconnect on the cord so this isn't such a hassle when I finally move to a better quality submersible.

    You guys are great! Thanks again. (Now I just have to figure out why my email notices didn't work for this thread!)
    - Darell
    HH180, Cutmaster 38, Miller Xlix Elite, TurnPro 7x12 Horiz bandsaw.

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